IRM now has another car in its operating fleet! Shaker Heights 18 was made operational and, after a few tentative voyages up and down the inspection pit lead, went for a couple of test trips around the streetcar line.
This progress was made much quicker than anticipated, but it's thanks to the hard work of the car shop regulars: Joel, Zach, Nick, Jeron, Greg, and Richard (I'm sorry if I left anyone out!). They brought the 18 over to the pit to look at the air compressor. That led to the compressor being dropped and new brushes being put in, but once it was meggered and reinstalled it was started up and surprisingly few leaks were found. All of the car's electrical circuits had already been tested so after the controls were sequenced the motor leads were hooked up and it was time for some testing.
Overall the car seems to run very nicely. There are a handful of small air leaks but nothing that can't be addressed. One bearing started to run a bit warm so we will repack that. We haven't been able to get the tail end marker lights working because the cast lens frames are cemented in place by rust and paint, but that will be taken care of.
Obviously there's more to do on the car. A lot of it is cosmetic: the car badly needs a new paint job, and volunteers from the Northern Ohio Railway Museum have been contacted about the correct color formula. It will need some more windows repaired, and that work is underway; needs some new destination sign glass; a few air system fixes; and longer-term will need the interior gone over and refurbished, with refreshed paint and varnish. We are also missing one short bench seat cushion. But generally everything looks promising. A huge THANK YOU to everyone who got car 18 running!
As usual, other projects are making noticeable progress too. The lean-to was a regular Highwood Shops, with a few different North Shore efforts in evidence. Here is the old train door and the new replacement train door for MD car 213. It must be the train door because the only other doors on the car are big baggage doors!
And these are the new end windows for the 757. By the end of the day the holes for the hardware and mounting strips had been drilled and the windows were ready for installation once some welding work on the support frames is done.
The North Shore Bandit returns - this week Zach was cutting out new linoleum for the floor in the smoker of the 757. The car has this patterned white linoleum under the seats, with a red walkway down the center aisle bordered by narrow black linoleum strips. When IRM acquired car 757 from East Troy the smoker linoleum had been replaced by some 1970s-era stuff, so in 2012 that was pulled out. After a few years of dormancy the compartment is now acquiring a new, correct, floor.
Zach also snapped a photo of me wire-wheeling trolley base parts for the 451. Many thanks to Zach, Joel, and Richard, who helped get parts we need out of storage including roof fuse boxes, a trolley hook, and a new trolley base spring.
6 comments:
Great report! It is good to once again be able to follow work at the IRM. Wish that I could be there.
That was awesome! That car moved along very nicely. Does this car need funding? Is the museum still encouraging all donations to the General fund during this Covid thing?
Glad you asked! The answer is yes, we can definitely use funding. The car doesn't have any money in its restoration fund and we will need to be able to buy paint and other supplies to get the car ready for public service. Donations can be sent in to Shaker Heights 18. Thank you to everyone who is able to contribute!
Frank- Although the lens on that switch/signal box is blue when viewed in sunlight, it will show a green light when lit by the yellowish light of an incandescent bulb. Regular green signal lenses are the same color.
R. W. Schauer
We had an issue with 1218 and a hot bearing at Trolleyville. It got hot during a special event and the motorman did not report the change in operation (squeeling). When we inspected the bearing after hearing it roll past the shop the babbit had already started to melt. A new one was poured and installed. If memory serves me correctly, we had a member of the Ohio Central steam shop (now age of steam roundhouse) come up and help in the process to make sure it was done correctly (they have done quite a few down there). Afterwards in tests the bearing still got too warm in a very short amount of time. All of the angles, alignments, and wear patterns still looked good after the tests, but it still got too hot for our comfort. A few of us had suspected that the car may be finding ground through only that bearing for some reason. The car was parked and the theory was never worked on before the museum folded. It was so long ago I can not remember exactly which axle it was.
Regarding Chris's theory about the bearing passing excessive ground current: I don't think it's likely to have been the problem here. Current passing through a bearing interface doesn't directly cause it to get hot; instead, it causes little pits and roughness in the surfaces, which can be seen by the time they're serious enough to cause trouble. I don't recall seeing that sort of thing here. Anyway, the car has had a number of "squealers" over the course of switching it from here to there, sometimes after moving backwards.
R. W. Schauer
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