I went out to the museum on Sunday to try and finish up the 309's inspection in preparation for operations on Monday. Charlie Strong and Stan Wdowikowski had completed most of the inspection work on the car, leaving me with only the contactor boxes and controller to examine. I did this (more information on contactor operation can be found in the next post down), finding no real issues, and sequenced the car successfully with help from Tim Peters. (Sequencing involves visual inspection of all contactors in operation - obviously with the motors cut out - to ensure proper operation.) The work wasn't quite done, though; Stan had found that the #4 motor had some oil on the commutator, which if left alone can lead to a flashover. He had cleaned up all of the oil during the week, though, and we were planning on taking the 309 out on a test trip on the main line to see if the problem was solved when something else caught our attention.
CTA streetcar 3142, which is our standard service streetcar and sees use virtually seven days a week from Memorial Day to Labor Day, suffered a motor failure in service. The failure occurred at Car Line Junction, tying up operations out of Station Track 1 until IT 415 was able to push 3142 onto the tail track. This deals a tough blow to the museum's streetcar operations; stay tuned for information on plans to get the motor sent out for repair.
Anyway, following this incident we did actually take the 309 out on the line for a trip, even carrying a full load of passengers. Upon our return the #4 motor was inspected again and more oil was found on the commutator, meaning that the car shouldn't be put into service until the cause of the oil leakage is found and repaired. The timeline for this is unknown since we don't know exactly where the source of the oil is, but the motor has not had any electrical issues so the fix ought to be something we can do in-house. Outside of the Car Shop, there was a lot of interesting stuff happening. The Nebraska Zephyr made its celebrated return today; the Electroliner was on display on the west track of 50th Avenue Station; the Track Crew was hard at work tamping and leveling the east track (pictured, L-R: Frank DeVries, Adam Robillard, unknown (back to camera), Tom Hunter, Steve L., John Neglich); and the last two C&NW-painted diesels owned by the UP even made a cameo appearance in Steamland.
News and views of progress at the Illinois Railway Museum
Monday, May 25, 2009
Motor Issues
Posted by Frank Hicks at 12:49 PM
Labels: 309 Progress
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2 comments:
Perhaps the 1374 or the 144 will see some more action in light of the 3142 motor failure...
That's likely; the 144 was on the inspection pit on Sunday and may go into semi-regular service in the near future. The 1374 is still likely to be held back from regular use because of ongoing issues with its K-28 controllers.
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